L79 rebuild in Dallas - NCRS Discussion Boards

L79 rebuild in Dallas

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  • Gary H.
    Frequent User
    • September 18, 2018
    • 69

    L79 rebuild in Dallas

    gary...

    1967
    Convertible, L79 327/350hp, M20, Marlboro Maroon (sort of) / Saddle
  • David H.
    Extremely Frequent Poster
    • June 30, 2001
    • 1574

    #2
    Re: L79 rebuild in Dallas

    Originally posted by Gary Hardy (65191)
    .... Now blowing smoke out of the left exhaust, clunky idle, dead miss, no power. ...
    Gary

    Color of smoke?

    Flat tappet or roller cam?

    Coolant in oil / oil in coolant?

    Appearance of spark plugs?

    Dave
    Judging Chairman Mid-Way USA (Kansas) Chapter

    Comment

    • Gary H.
      Frequent User
      • September 18, 2018
      • 69

      #3
      Re: L79 rebuild in Dallas

      Should have pulled the valve covers first. OOPS! Suggestion on method to pull the stud.

      IMG_6487.jpg
      gary...

      1967
      Convertible, L79 327/350hp, M20, Marlboro Maroon (sort of) / Saddle

      Comment

      • Leif A.
        Extremely Frequent Poster
        • August 31, 1997
        • 3658

        #4
        Re: L79 rebuild in Dallas

        Gary,
        That's better news. Let's see a picture of the broken stud in the head. There may be enough to grab. If not, this is still going to be easier and WAY cheaper than the alternative.
        Leif
        '67 Coupe L79, M21, C60, N14, N40, J50, A31, U69, A01, QB1
        Top Flight 2017 Lone Star Regional

        Comment

        • Bill M.
          Extremely Frequent Poster
          • July 31, 1989
          • 1332

          #5

          Comment

          • Tim G.
            Extremely Frequent Poster
            • March 1, 1990
            • 1424

            #6
            Re: L79 rebuild in Dallas

            Gary, it looks like the push rod is still in place, that's also very good.

            Comment

            • Gary H.
              Frequent User
              • September 18, 2018
              • 69

              #7
              Re: L79 rebuild in Dallas

              Originally posted by Leif Anderson (29632)
              Gary,
              That's better news. Let's see a picture of the broken stud in the head. There may be enough to grab. If not, this is still going to be easier and WAY cheaper than the alternative.
              I'm going with using a die to thread the remaining stud. Then using a nut to pull it. Then tapping in a new stud.
              gary...

              1967
              Convertible, L79 327/350hp, M20, Marlboro Maroon (sort of) / Saddle

              Comment

              • Mark E.
                Extremely Frequent Poster
                • April 1, 1993
                • 4614

                #8
                Re: L79 rebuild in Dallas

                What's the cause of this? It looks like the rocker stud AND the rocker arm broke.

                Did the rocker stud fail, which somehow broke the rocker arm? Or the other way around? Did the valve hit the piston? Over revving?

                It's curious the pushrod remained in place. It seems more likely the lifter would push out of its bore. The pushrod must have made a LOT of noise bouncing against the valve cover.
                Mark Edmondson
                Dallas, Texas
                Texas Chapter

                1970 Coupe, Donnybrooke Green, Light Saddle LS5 M20 A31 C60 G81 N37 N40 UA6 U79
                1993 Coupe, 40th Anniversary, 6-speed, PEG 1, FX3, CD, Bronze Top

                Comment

                • Tom D.
                  Extremely Frequent Poster
                  • September 30, 1981
                  • 2151

                  #9
                  Re: L79 rebuild in Dallas

                  It looks as if the push-rod is no longer on the lifter. Looks angled on the top end.
                  https://MichiganNCRS.org
                  Michigan Chapter
                  Tom Dingman

                  Comment

                  • Gary H.
                    Frequent User
                    • September 18, 2018
                    • 69

                    #10
                    Re: L79 rebuild in Dallas

                    Originally posted by Mark Edmondson (22468)
                    What's the cause of this? It looks like the rocker stud AND the rocker arm broke.

                    Did the rocker stud fail, which somehow broke the rocker arm? Or the other way around? Did the valve hit the piston? Over revving?

                    It's curious the pushrod remained in place. It seems more likely the lifter would push out of its bore. The pushrod must have made a LOT of noise bouncing against the valve cover.
                    It looks like the stud just snapped. No clue why. Rocker is fine. The spring was in place so the valve never dropped. Yea. It was making a hell of a noise by time I got home. I'll post the final result after I replace the stud and adjust the rocker.
                    gary...

                    1967
                    Convertible, L79 327/350hp, M20, Marlboro Maroon (sort of) / Saddle

                    Comment

                    • Gary H.
                      Frequent User
                      • September 18, 2018
                      • 69

                      #11
                      Re: L79 rebuild in Dallas

                      Originally posted by Leif Anderson (29632)
                      Gary,
                      That's better news. Let's see a picture of the broken stud in the head. There may be enough to grab. If not, this is still going to be easier and WAY cheaper than the alternative.
                      Absolutely enough stud to try my rethread with die and pull idea.
                      IMG_6488.jpg
                      gary...

                      1967
                      Convertible, L79 327/350hp, M20, Marlboro Maroon (sort of) / Saddle

                      Comment

                      • Mark E.
                        Extremely Frequent Poster
                        • April 1, 1993
                        • 4614

                        #12
                        Re: L79 rebuild in Dallas

                        So the rocker arm is ok but the rocker stud broke. Maybe a bent pushrod, or the stud suffered metal fatigue or was defective? If the pushrod is bent, consider checking, maybe replacing all the pushrods (if not done during the recent head work). If the rocker stud just mysteriously broke, consider checking, maybe replacing all the studs.

                        Is the lifter still in its bore?
                        Mark Edmondson
                        Dallas, Texas
                        Texas Chapter

                        1970 Coupe, Donnybrooke Green, Light Saddle LS5 M20 A31 C60 G81 N37 N40 UA6 U79
                        1993 Coupe, 40th Anniversary, 6-speed, PEG 1, FX3, CD, Bronze Top

                        Comment

                        • Duke W.
                          Beyond Control Poster
                          • January 1, 1993
                          • 15706

                          #13
                          Re: L79 rebuild in Dallas

                          A close up photo of both sides of the break might reveal a cause.

                          The stud is subject to cyclic loading so fatigue can be an issue. Fatigue failures usually start with a small surface flaw. Then the cyclic loading causes the flaw to propagate as a crack. Once the crack has weakened the part sufficiently, it will suddenly fail. Most connecting rod failures are due to fatigue, but bearing seizure can also break rods due to the huge bending load placed on the rod as the bearing seizes up, and the failure is often about one third the way up from the big end.

                          A fatigue failure will usually show a relatively smooth area, which is the progress of the crack. Then the rest of the section where the final sudden break occurs will have a comparatively rougher finish.

                          The above is a classic fatigue failure script for a cyclically loaded part.

                          Duke

                          Comment

                          • Gary H.
                            Frequent User
                            • September 18, 2018
                            • 69

                            #14
                            Re: L79 rebuild in Dallas

                            Originally posted by Duke Williams (22045)
                            A close up photo of both sides of the break might reveal a cause.

                            The stud is subject to cyclic loading so fatigue can be an issue. Fatigue failures usually start with a small surface flaw. Then the cyclic loading causes the flaw to propagate as a crack. Once the crack has weakened the part sufficiently, it will suddenly fail. Most connecting rod failures are due to fatigue, but bearing seizure can also break rods due to the huge bending load placed on the rod as the bearing seizes up, and the failure is often about one third the way up from the big end.

                            A fatigue failure will usually show a relatively smooth area, which is the progress of the crack. Then the rest of the section where the final sudden break occurs will have a comparatively rougher finish.

                            The above is a classic fatigue failure script for a cyclically loaded part.

                            Duke
                            I think it's that simple.
                            gary...

                            1967
                            Convertible, L79 327/350hp, M20, Marlboro Maroon (sort of) / Saddle

                            Comment

                            • Gary H.
                              Frequent User
                              • September 18, 2018
                              • 69

                              #15
                              Re: L79 rebuild in Dallas

                              Well... it wasn't that simple. I went the rebuild route. I found Engine Rebuilders in Dallas. Check them out; the shop, builds at various stages, some of the guys, online reviews. They seemed okay. Before I dropped it off (and when I dropped it off) I told them, please do not touch the block stamp in any way. It was clearly communicated to the owner and the manager. You see where I'm going. They didn't communicate it to the shop. So! They didn't completely grind off the stamp, but, it's pretty bad now. Here are the pics (original and now). How bad is this?

                              original.jpgnow.jpg
                              gary...

                              1967
                              Convertible, L79 327/350hp, M20, Marlboro Maroon (sort of) / Saddle

                              Comment

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