Re: 1964 FI Roadster
You have to be careful as there are several different ways to measure horsepower. In my experience, a "stock rebuild" will be about 10 percent short of the advertised SAE gross horsepower/torque at about 10 percent less revs. Massaging the heads will get pretty close to the OE SAE gross numbers. SAE gross uses the "standard temperature/pressure (STP)air density correction factor, which is 29.92" Hg, 59F, zero humidity and is the defacto air density correction method for aftermarket lab dyno tests.
Various correction factors can be applied... DIN, JIS... but current SAE net correction uses lower temperature/pressure than STP, which reduces torque /power data by about 4.5 percent compared to STP. SAE net should also be applied to RWHP test data.
Another issue is headers versus manifolds. If you plan to run manifolds on the car, use manifolds for the lab dyno test. One lab test session I have where both headers and OE manifolds were used showed about 8 percent more peak torque, but only about 3 percent more top end power, and, of course, that would be with no mufflers on either. With the OE exhaust system the differences will be less.
I have yet to see a SHP/FI 327 make over 300 SAE corrected RWHP, but with massaged heads they come close. Peak power is usually at about 6500 with a little rolloff to 7000+.
You need to let these short stroke engines rev, which is why I say you are nuts if using OE connecting rods, especially the pre-'66 versions that are decidedly weak at the bolts seats and have destroyed many blocks when they let go over the years.
During a chassis dyno test you need to ensure that the fan clutch does not tighten, which can cost up to about 10 lb-ft and 15 horsepower... best to test on a cool day, make sure the shop has good external cooling fans, and bring a garden sprayer to spritz down the radiator between pulls. If you post data, please provide full context like correction factor type, headers or manifolds, and whether an electric or mechanically engine water pump was used. It's usually assumed that no mufflers are installed in the lab exhaust evacuation system.
I have a written chassis dyno test plan. If anyone is interested, contact with via email through the TDB.
Duke
You have to be careful as there are several different ways to measure horsepower. In my experience, a "stock rebuild" will be about 10 percent short of the advertised SAE gross horsepower/torque at about 10 percent less revs. Massaging the heads will get pretty close to the OE SAE gross numbers. SAE gross uses the "standard temperature/pressure (STP)air density correction factor, which is 29.92" Hg, 59F, zero humidity and is the defacto air density correction method for aftermarket lab dyno tests.
Various correction factors can be applied... DIN, JIS... but current SAE net correction uses lower temperature/pressure than STP, which reduces torque /power data by about 4.5 percent compared to STP. SAE net should also be applied to RWHP test data.
Another issue is headers versus manifolds. If you plan to run manifolds on the car, use manifolds for the lab dyno test. One lab test session I have where both headers and OE manifolds were used showed about 8 percent more peak torque, but only about 3 percent more top end power, and, of course, that would be with no mufflers on either. With the OE exhaust system the differences will be less.
I have yet to see a SHP/FI 327 make over 300 SAE corrected RWHP, but with massaged heads they come close. Peak power is usually at about 6500 with a little rolloff to 7000+.
You need to let these short stroke engines rev, which is why I say you are nuts if using OE connecting rods, especially the pre-'66 versions that are decidedly weak at the bolts seats and have destroyed many blocks when they let go over the years.
During a chassis dyno test you need to ensure that the fan clutch does not tighten, which can cost up to about 10 lb-ft and 15 horsepower... best to test on a cool day, make sure the shop has good external cooling fans, and bring a garden sprayer to spritz down the radiator between pulls. If you post data, please provide full context like correction factor type, headers or manifolds, and whether an electric or mechanically engine water pump was used. It's usually assumed that no mufflers are installed in the lab exhaust evacuation system.
I have a written chassis dyno test plan. If anyone is interested, contact with via email through the TDB.
Duke
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